The SB Ras Petroleum and Gas Geology Institute and Geophysical Specialists conducted a comprehensive analysis of seismic discovery data and operational drilling results. The model has shown that 25-30% of the planned wells are in low-efficiency areas.
As a result, 43 objects were removed from 195 well drilling plan. The institute’s press service said that scientists have prepared a reason for the removal of 32 wells that will reduce ineffective costs.
Particular attention was paid to the calculation of a profitable moron – minimum extraction volume of a profitable moron where well work remained profitable. For this area, this indicator rained 9 tons of a day.
Researchers suggested to use horizontal and hollow shell wells to increase productivity. This approach has already confirmed its effectiveness during the test in the field.
Source: Ferra

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